High burning temperature experiment on pintle controlled solid motor

Jia Xing Wang*, Zhi Jun Wei, Ning Fei Wang

*此作品的通讯作者

科研成果: 期刊稿件文章同行评审

14 引用 (Scopus)

摘要

In order to investigate the performance of pintle controlled solid rocket motor under the condition of high burning temperature, a coaxial pintle solid motor system was designed, with a linear motor as pintle actuator. Under this system, an experiment was carried out using modified double base propellant with high burning temperature and high pressure exponent. The chamber pressure was changed from 12.1~2MPa. It was found that pintle head was eroded seriously, and it reduced interior ballistics precision greatly. Relevant solutions were recommended to reduce this detrimental influence, such as adopting close loop control, increasing pintle diameter, choosing appropriate propellant and so on. This could provide some experience and foundation for pintle controlled solid motor design in future.

源语言英语
页(从-至)89-92
页数4
期刊Tuijin Jishu/Journal of Propulsion Technology
33
1
出版状态已出版 - 2月 2012

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