双脉冲固体火箭发动机脉冲隔离装置设计与试验

Kai Mei*, Jun Wei Li, Zhong Wang, Ning Fei Wang

*此作品的通讯作者

科研成果: 期刊稿件文章同行评审

3 引用 (Scopus)

摘要

In order to improve the energy efficiency of solid rocket motors, a pulse separation device (PSD) with plug-in board and plug as the main structure is designed. This device is different from the traditional PSD, in which the material for plug-in board is tungsten infiltration of cooper and the plug is Polyoxymethylene(POM) or Polycaprolactam (MC). PSD achieves separation of the combustion chamber of the motor with its simple construction. The bursting pressure of plugs of different materials are tested by the hydraulic test, and the results are in good agreement with theoretical calculations. POM and MC can withstand pressure above 20MPa and open smoothly during the two-pulse operation. The bursting pressure of POM is 39.8MPa. The test results prove that PSD is feasible and has excellent reliability in double-pulse solid rocket motor.

投稿的翻译标题Design and Experiment of Pulse Separation Device of Double Pulse Solid Rocket Motor
源语言繁体中文
页(从-至)758-766
页数9
期刊Tuijin Jishu/Journal of Propulsion Technology
41
4
DOI
出版状态已出版 - 1 4月 2020

关键词

  • Double-pulse solid rocket motor
  • Energy management
  • Hydraulic test
  • Pulse separation device

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