TY - GEN
T1 - Analysis of the cool bending fracture of HRB400
AU - She, Yuan
AU - Kong, Wei Ming
AU - Zhang, Zhao Hui
N1 - Publisher Copyright:
© (2014) Trans Tech Publications, Switzerland.
PY - 2014
Y1 - 2014
N2 - The tests were conducted on 400MPa hot-rolled ribbed bar(HRB400). The cool bending fracture appeared frequently in the production was analyzed. The research result showed that the cool bending fracture of rebar were caused by element segregation of C, Mn, inclusions, the existence of banded structure, widmannstatten structure and bainite structure in the center and edge of rebar. The inclusions are the root cause of internal crack and one of the reasons to fracture. Reasonable cooling rate can refine grain size, while the overquick cooling speed could result in the formation of widmannstatten structure in acicular or plume, increased the brittleness of steel and reduce its cold bending properties. On this basis, some improvement opinions were put forward: using the raw material with low Mn, S and P; reducing the S content with pretreatment of hot metal; controlling the content of C and Mn respectively in C: 0.18 ~ 0.23%, Mn:1.20~1.30%; extending argon blowing time at argon flushing station, using electromagnetic stirring technology; controlling the cooling rate at 15 ℃/s.
AB - The tests were conducted on 400MPa hot-rolled ribbed bar(HRB400). The cool bending fracture appeared frequently in the production was analyzed. The research result showed that the cool bending fracture of rebar were caused by element segregation of C, Mn, inclusions, the existence of banded structure, widmannstatten structure and bainite structure in the center and edge of rebar. The inclusions are the root cause of internal crack and one of the reasons to fracture. Reasonable cooling rate can refine grain size, while the overquick cooling speed could result in the formation of widmannstatten structure in acicular or plume, increased the brittleness of steel and reduce its cold bending properties. On this basis, some improvement opinions were put forward: using the raw material with low Mn, S and P; reducing the S content with pretreatment of hot metal; controlling the content of C and Mn respectively in C: 0.18 ~ 0.23%, Mn:1.20~1.30%; extending argon blowing time at argon flushing station, using electromagnetic stirring technology; controlling the cooling rate at 15 ℃/s.
KW - Cool bending fracture
KW - Cooling rate
KW - Inclusions
KW - Segregation
UR - http://www.scopus.com/inward/record.url?scp=84912079245&partnerID=8YFLogxK
U2 - 10.4028/www.scientific.net/AMR.1028.50
DO - 10.4028/www.scientific.net/AMR.1028.50
M3 - Conference contribution
AN - SCOPUS:84912079245
T3 - Advanced Materials Research
SP - 50
EP - 54
BT - Designing of Industrial Facilities and Technologies
A2 - Zeng, Dehuai
PB - Trans Tech Publications Ltd.
T2 - International Conference on Algebraic and Complex Geometry
Y2 - 10 September 2012 through 14 September 2012
ER -