摘要
The paper reveals the effects of the group delay in a digital filter on the stability of an active flutter suppression system for a 2 dimensional airfoil section. The wind tunnel tests show that the active flutter suppression system becomes unstable at very slow flow speed if the group delay of the digital filter is long enough. In the wind tunnel tests of flutter suppression, the flutter amplitude under control often decreases at first as expected, and then the other self-excited vibration with lower frequency and moderated amplitude appears. The paper well explains such a phenomenon through a combined theoretical and numerical study. Both wind tunnel tests and numerical simulations demonstrate that the group delay greatly affects the above unstable motion, and that both the amplitude and frequency of the new self-excited vibration will increase with the group delay.
| 源语言 | 英语 |
|---|---|
| 页(从-至) | 153-159 |
| 页数 | 7 |
| 期刊 | Zhendong Gongcheng Xuebao/Journal of Vibration Engineering |
| 卷 | 26 |
| 期 | 2 |
| 出版状态 | 已出版 - 4月 2013 |
| 已对外发布 | 是 |
指纹
探究 'Effects of group delay in digital filter on stability of an active flutter suppression system' 的科研主题。它们共同构成独一无二的指纹。引用此
- APA
- Author
- BIBTEX
- Harvard
- Standard
- RIS
- Vancouver